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Eastgate Drainage Study I I I I I I I I I I I I I I I I II I I EASTGATE DRAINAGE STUDY Dow Addition City of Salina, Kansas Mayor Peter F. Brungardt City Commissioners John Divine Joseph A. Wamer Carol E. Beggs Evelyn Maxwell City Manager Dennis M. Kissinger Director of Engineering & Utilities Don Hoff: P.E. November 1993 Project No, 10-93142-31 EARLES & RIGGS Engineers, Planners, and Landscape Architects Post Office Box 147 Lindsborg, Kansas 67456 (913) 227-3787 - Fax (913) 227-3788 ",II""'".. . ", "', tll ", .(~R 11. fA ð '1# " ~ \ ....... 'T/ þ"" ..' /"IV.. .0 <'<.-, .. :l '... \cENSE'o ...ú' ""-;. .. . " '.. , . . .. t r 10393 ~~ ~J W~ vJ ¿~4Jc ';.~ -0 ..0 /¥/~9 5' ... Q:- .-:: "'.. -P.o .. ~ ~NS "C',;) .' L4J ,'~ . ~ .. .0 ..:>,.v, '. I;. ......" G'~ " "..,~SION Al E.~"..., ',. .-.."",., I I I I I I I I I I I I I I ! I I I I I Eastgate Drainage Study Table of Contents Purpose page 2 Background page 2 Act~al Construction page 2 Problems page 3 Discussion Page 3 Solutions Page 4 Typical Ditch X-Section Page 5 Costs Page 6 Appendix A - Original Storm Drainage Plan Appendix B - Existing Ditch Plan & Profile Appendix C - Existing Ditch X-Sections Eastgate Drainage Study page 1 I I I I I I I I I I I I I I I I I I I EASTGATE DRAINAGE CIIT OF SALINA E&R File 10-93142-31 Purpose: To provide a reasonable solution to the drainage problems associated with the holding pond and ditch located in the Dow Addition to the City of Salina. Background: The original drainage study was completed in 1984 by Appleby Architects. This study focused on the area bounded by Cloud Street on the south, Braidshaw Street to the north, Ohio Street to the West and the east extends of the Dow Addition to the east (see layout in Appendix A). The entire area was laid out to drain into an existing drainage swale located on the east edge of the Dow Addition which drains into a 42-inch diameter pipe running through the Smoky Hill River dike. To control the volume of run-off: a holding pond was constructed and sized to detain the runoff differential from a 10 year storm. The pond was designed to be emptied by pumping the storm water into the drainage ditch located on the eastern edge of the Dow Addition. A box culvert was to be installed between the pond and the ditch to act as on overflow device preventing the pond from over topping the street if the pumps were to fail. The existing drainage swale was then to be widened to a 30 foot ditch from Courtney Street east along the south side of the Dow Addition, approximately 550 feet, and then east along the east edge of the Dow Addition for approximately 1300 feet to north edge of the Dow Addition. The remaining 580 feet of drainage swale, which carries the flow to the 42-inch pipe, was to be widened in the future. This ditch was to be graded at a slope of 0.05 % and to flow at a depth of approximately two feet in order to carry the required volume of runoff. The drainage pattern for the area was to have Minneapolis Street drain directly into the pond. Bradshaw and Beloit Streets would drain into the northern portion of East gate Drive and flow through a flume inlet directly into the newly widened ditch, Louis Lane would drain to the east into Courtney Street which drains south into the drainage ditch. Ellsworth Street would drain into the southern portion of East gate Drive, through another flume inlet and into the newly widened ditch. Actual Construction: The ditch was constructed with a 20 foot bottom width at a slope of 0.05%, or 5/8 inch drop in 100 feet. This widen ditch section was installed from just east of Courtney Street, east to the east edge of the Dow addition, then north along the eastern edge of the Dow Addition to the northern edge of the Dow Addition. The remaining 580 feet north to the 42" pipe remained a V-ditch. The two flumes were installed as stated, one on the south portion of East gate Drive and one on the north. The top of the flumes were constructed at elevation 1221.78 for the south flume and 1221.88 for the north flume. Eastgate Drainage Study page 2 I I I I I I I I I I I I I !I I I I I I The pond was constructed with a capacity of3.4 acre-feet of storage below the 1221.00 elevation. A concrete flume was constructed which runs the length of the pond's center and empties into the lift station. The flow line of the flume at the lift station is 1217.00, with the floor of the lift station at elevation 1211.83. When the water in the wet well reaches three feet in depth or at elevation 1214.83 the discharge pumps automatically switch on and discharge into a double cell2'x4' reinforced box culvert constructed between the pond and the ditch under Eastgate Drive, which carries the flow into the drainage ditch. The inflow elevation of this box, pond side, is 1220.85, with the discharge elevation into the ditch at elevation 1220.68. There are two inlets constructed into the top of the box which allows the flow along Eastgate Drive to drain into the box. Problems: A normal minimum grade required to maintain flow and prevent silting in a grass lined ditch is 0.40%. The current grade of the Eastgate ditch is 0.05%, considerable less than the acceptable standard. This low grade is part of the cause for some of the ponding, however the main reason for the ponding is the condition and width of the ditch from the north edge of the Dow Addition north to the dike. The ditch abruptly goes from a 20 foot flat-bottom ditch to a v-ditch at the north edge of the property. The v-ditch then continues 580 feet to the dike with a grade that varies, but at times is as much as one foot higher than the flow line of the widened ditch forcing the water to pond a foot in depth in the Eastgate area before flowing on to the dike. (See Appendix B and Appendix C) In order for the widened ditch to carry the required flow at a slope of 0.05%, the original calculations, which were based on using a 30 foot flat bottom ditch, show the depth of the water to be approximately two feet, assuming no blockage of the ditch. The actual existing ditch flow lines and flume inlets were surveyed to find out the actual allowable depth that could occur in the ditch before it flooded the roadway. We found the roadway elevation near the south flume inlet on Eastgate Drive was at elevation 1221. 78 and the ditch elevation was 1221.0. At the north flume the roadway elevation was 1221.88 and the ditch elevation was 1220.5. These elevations at the ditch flow lines with reference to the street flow lines and the required depth of flow, readily show another reason for the flooding. The water level in the ditch need only rise one foot and the water is flooding Eastgate Drive. Adding to the flooding problem are the pond pumps which turn on immediately upon receipt of water into the pond. The water is pumped into the west end of the reinforced box culvert which drains into the ditch. Presently the flow line of the box culvert is approximately equal to the flow line of the ditch. As the water backs up in the ditch, the water overflows through the box culvert and flows into the pond. At the same time the pumps are running, pumping the water into the ditch, and the circulation of water begins. Another concern is the river. When the Smoky Hill River rises, the flap gate at the end of the 42-inch pipe under the dike is closed and no flow will exit this ditch. There is currently no other way to get the flow through the dike. Eastgate Drainage Study page 3 I I I I I I I I I I I. I I I I I I I I Discussion: The survey showed that unless the 42-inch discharge pipe was lowered, the maximum slope that can be maintained in this ditch from Courtney Street to the pipe is 0.05%. Looking at the roadway elevations in comparison to the ditch grades, it is also apparent that the maximum depth of flow allowable before street flooding occurs is 1 to 1.5 feet. In order to obtain the quantity offlow required, realizing that the slope must remain the same and the depth of flow is limited, the width should be adjusted to create a larger flow area or a larger holding area must be created to reduce the volume of flow. In order to maintain the greatest flow in the ditch, the ditch should be keep as wide as possible throughout it's length and the pond used as a storage and overflow basin. It is our recommendation that the current v-ditch be widened to a minimum of a 20 foot flat bottom ditch with 2 to 1 side slopes (see new ditch x-section on the following page). To reduce the flow in the drainage ditch we suggest the pond's pumps not discharge water into the ditch until the ditch flow has been reduced by flowing through the 42-inch discharge pipe. This could be accomplished by use of a time delay switch on the pond pumps, however this would require some additional water storage capability. In order to get the maximum use of the pond, we suggest deepening the pond to the maximum allowed by the water table. If the pond is deepen to elevation 1217.00, the storage volume below elevation 1221.00 would increase from 3.4 acre-feet to 5.5 acre- feet, thus allowing for more storage which would elevate some of the flooding problems in this area. When the river rises and the pipe discharge is sealed, water will rise in both the ditch and the pond simultaneously. Once the water elevation reached 1221.00 the water would begin to flow onto the roadway. The only way to eliminate the problem would be to pump the runoff from the pond over the dike to the river. Solutions Short Term: 1.) Widen north end of ditch from the north edge of the Dow Addition, north to the dike. Required - City will be required to purchase 60 feet of drainage easement, assuming a 20 foot flat-bottom ditch with 2 to 1 side slopes 2.) Widen and deepen the pond below elevation 1221.00 to provide additional storage capacity. Required - Removal of concrete flume through the center of the pond 3.) Install time delay switch to pond discharge pumps Required - Adjustment of discharge pump's high level alarm Long Term: 1.) Extend pump discharge line over the dike Required - Establishment of a drainage district and two discharge p!lffiPS . Eastgäte Dramage Study page 4 ------------------- Typical Ditch X-Section 20' Eastga te Drainag.s¿ Ditch (Iypj Easlgalc Drainage Study page 5 I I I I I I I I I I I I I I I I I I I Costs: Short Term: Item Excavation Concrete Removal Ditch Liner Pump Delay Switch Quantity Unit Cost 6200 C.Y. $ 5.00 84 C.Y. $ 30.00 70 S.Y. $ 45.00 1 Each $500.00 Subtotal 15% Contingency Cost $31,000.00 $ 2,520.00 $ 3,150.00 $ 500.00 $37,170.00 $ 5.575.00 $42,745.00 $ 8.549.00 $51,294.00 Long Term: Costs will vary depending on the volume of water pumped. If the current wet well can be reused and only the pumps replaced and a new discharge line installed, the total cost could run around $45,000 to $65,000. If the city decided to pump at a much higher rate, the costs for a completely new lift station could run between $130,000 to $250,000 depending on the size and availability of the discharge pumps. Engineering, Legal, Bonds and Administration (20%) Total Estimate Probable Cost Eastgate Drainage Study page 6 I I I I I I I I I I I I I I I I I I I APPEND IX A ORIGINAL STORM DRAINAGE PLAN ¡ ¡ Dit!h ~ -rr., .,i I r. I . /! J - , ¡ . ~.:. I ~ * , j ë -~--- . I tEL, 121°,68 El. Ij~~~ ,,~lIL._L_- ._-~ " , """"""""",' "",~." )/ . - EASTGATE DRlVE- "'"\'.. ./ ~ " ,/ ,~ / :ì~ / . ~¡---~ I ./ I $ ,/ f ¡ I' I- f / ~ ! j . I I ¡ I ~ 1 { . ~ f . ¡..~.... .. ---"----1 ~ .' ~ ~ ; ¡ i I i i í i ~ I I ¡ $ < I I i I t I ¡ f.""'4"d~'.'.."'..'.'l...'~"""'-'~~""-.r' f ~, i. >F'-""""".'--'.<. t ! ~ ¡ I i i ~ ¡ i ~ ) ~ ~ 1 i ~ ¡ ~ ~ ¡ ~ i ~ l ,,¡ !i---»,._,~------i j Ii ~.~. """..""",.--,~ I " ~ ;' ~ ~ - r v i , " . ~ ~ - ¡ ; '..'.M ..,.1 ~ rJ) EARLES &j RIGGS ~ ENGINEERS. 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